A derailment and explosion in a CN Rail marshalling
yard in Prince George 18 months ago is being blamed
on a lack of training among management staff and
rail cars that were too heavy.
A report released by the Transportation Safety Board
(RAILWAY
INVESTIGATION REPORT R07V0213) Tuesday found that managers operating a remote
control switching system when the explosion occurred
on Aug. 4, 2007, weren't properly trained for the
duties they were performing.
"Although considered qualified from a regulatory
perspective for their respective duties, the
management employees . . . were inadequately trained
and had no experience switching long, heavy cuts of
cars on this particular piece of track," said board
investigator Peter Hickli.
The accident involved a CN supervisor losing control
over a 53-car remote controlled train, which struck
another train pulling cars loaded with gasoline. The
crash caused a derailment, explosion and fire.
"The collision occurred when the excessive tonnage
of the 53 cars and the descending track gradient . .
. combined to exceed the braking capacity of the
switching locomotives," Hickli said.
No one was hurt but 172,000 litres of gasoline and
diesel spilled, most of which burned in the fire.
Kelli Svendsen, spokeswoman for CN, said the company
has been working diligently since the derailment to
improve the safety of its railroad and employees.
"In 2008, CN had a 30 per cent reduction in overall
accidents in Canada than in 2007 and we're seeing
this trend continue in 2009," she said.
Svendsen denied the board's finding that the
employees were inadequately trained for their duties
at the time of the derailment.
"In CN's view, the employees were experienced, they
were well-rested, and they were trained to perform
the duties that they were performing. The TSB did
note that the employees were considered qualified
from a regulatory perspective."
When pressed on whether the employees could be
qualified for the duties they were performing from a
regulatory standpoint while still lacking the
experience to perform those duties seamlessly,
Svendsen reiterated the company's belief that
experience was not a factor in the derailment.
The board also found that a risk assessment
conducted immediately prior to the accident was
inadequate to identify the hazards and mitigate the
risks of switching long, heavy cuts of cars on the
pull-back track's descending grade.
While the board report made no formal
recommendations in its report, it said "the practice
of temporarily assigning management employees to do
the work of experienced operating employees may
increase the risk of accidents."
The safety board went on to say that the lack of a
formal quality assurance program to establish
consistency in risk analyses increases the
likelihood that the controls identified and
implemented may not be sufficient to address the
risks.